NABABAN, POSMAN SUNARYO (2025) EVALUASI PENGGUNAAN TAIL SCREEN ROD PUMP UNTUK MENEKAN PREMATURE FAILURE PASCA JOB WELL SERVICE SUMUR “DURI A13-8”– LAPANGAN DURI. Tesis thesis, UPN Veteran Yogyakarta.
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Abstract
ABSTRAK
Premature failure pada rod pump menjadi permasalahan utama di Sumur
“DURI A13-8” akibat kondisi formasi unconsolidated sandstone yang
menyebabkan produksi pasir (sand production) berlebih dan merusak komponen
pompa. Dampak yang ditimbulkan meliputi downtime produksi sebesar 390 barel
serta peningkatan biaya operasional hingga 9.516 US$. Upaya clean out pasir dan
pemasangan rod pump baru belum efektif karena kegagalan kembali terjadi dalam
waktu kurang dari 30 hari.
Solusi yang diterapkan adalah desain ulang sistem rod pump dengan
penambahan tail screen sebagai penyaring pasir. Sampel pasir hasil clean out
dianalisis menggunakan sieve shaker sebanyak 200 gram. Hasil sieve analysis
menunjukkan D50 sebesar 0,42 mm dengan distribusi ukuran pasir 250–420
mikron. Berdasarkan metode Gillespie, dipilih slot screen 150 mikron yang berada
pada rentang D40–D70 untuk menjamin terbentuknya bridging effect tanpa
menurunkan laju alir fluida. Desain ini dilengkapi safety joint berkapasitas 60.000
lbf (12 shear pin) yang memungkinkan pemisahan tubing saat terjadi pump stuck
tanpa memerlukan rig workover.
Sebelum pemasangan tail screen, sumur DURI A13-8 mengalami empat
kali kegagalan pompa dalam setahun dengan downtime mencapai 60 hari dan
kerugian operasional signifikan. Setelah desain tail screen diterapkan—dengan
slot 150 mikron, open flow area optimal, dan penempatan tepat di zona perforasi
downtime berhasil ditekan menjadi hanya 0,5 hari, dan produksi stabil di 24
BOPD. Evaluasi keekonomian mencatat penghematan biaya hingga US$ 22.620
per kejadian, dibandingkan potensi kerugian US$ 40.468 tanpa safety joint.
Inovasi ini terbukti efektif secara teknis dan ekonomis dalam menangani
kepasiran dan memperpanjang usia rod pump.
Kata kunci: rod pump, sand production, tail screen, sieve analysis, safety
joint.
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ABSTRACT
Premature failure of the rod pump is a major issue in Well “DURI A13-8”
due to the unconsolidated sandstone formation, which causes excessive sand
production and damages pump components. The impact includes a production
downtime of 390 barrels and an increase in operational costs reaching IDR
172,011,816. Conventional mitigation such as sand clean-out and rod pump
replacement has proven ineffective, as failures repeatedly occurred within 30 days
after well servicing.
This study proposes a technical solution by redesigning the rod pump
system with the addition of a tail screen to filter formation sand. A 200-gram sand
sample obtained from clean-out was analyzed using a sieve shaker. The sieve
analysis showed a dominant particle size distribution in the 250–420 micron range,
with a D50 of 0.42 mm. Using the Gillespie method, a 150-micron slot screen was
selected within the D40–D70 range to ensure optimal bridging effect without
reducing fluid flow. The design also incorporated a 60,000 lbf safety joint (12 shear
pins) to enable tubing separation during pump stuck conditions without requiring a
rig-based workover.
Before the installation of the tail screen, Well DURI A13-8 experienced four
pump failures within a year, resulting in a total downtime of 60 days and significant
operational losses. After implementing the tail screen design—with 150-micron slot
size, optimized open flow area, and precise placement at the perforated zone—
downtime was reduced to just 0.5 days, while production remained stable at 24
BOPD. Economic evaluation showed a cost saving of up to US$ 22,620 per event,
compared to a potential loss of US$ 40,468 without the safety joint. This innovation
has proven to be technically and economically effective in addressing sand
production and extending the operational life of the rod pump.
Keywords: rod pump, sand production, tail screen, sieve analysis, safety
joint
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| Item Type: | Tugas Akhir (Tesis) |
|---|---|
| Uncontrolled Keywords: | rod pump, sand production, tail screen, sieve analysis, safety joint. |
| Subjek: | T Technology > T Technology (General) |
| Divisions: | Fakultas Teknologi Mineral dan Energi > (S2) Magister Teknik Perminyakan |
| Depositing User: | Eko Yuli |
| Date Deposited: | 27 Nov 2025 02:23 |
| Last Modified: | 27 Nov 2025 02:23 |
| URI: | http://eprints.upnyk.ac.id/id/eprint/45864 |
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